Dnepr - Ural - IZH - Voskhod - Minsk

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CHAPTER THREE - 14

Having been pleased with the seat I thought I had achieved a large jump forward, but I was disappointed (putting it mildly) when I went to do the final tightening of the gearbox to the engine. I had just fitted the lug for the clutch cable to fit onto, the one on the right ride that fits on the stud for the engine and gearbox. Having fitted it and tightened up the nut I thought that I had better check the other nuts holding the gearbox on. Off I go with my trusty spanner, tightening everything I see, when I get to the top nut, gave it a tweak until the nut was tight, then gave it a final twist, all of a sudden it went loose. Yes – you got it! I stripped the thread, but not on the nut, it had to be the thread inside the housing on the engine.

Many words were spoken when I realised what I had done, but it only really dawned on me as to the problem that I had when I tried to take out the stud. I thought that it would just pull out, but no I hadn’t thought that the other end of the stud was fatter than the top half. The only way to get this sorted was to take out the engine again. Once I‘d stopped crying!! I got on with taking out the engine, which was not easy, as I had to be careful not to chip and scratch the paint on the frame. Again out came the trusty pipe lagging and wrapped the frame up again. I had to take out the diff first, which now was quite easy as once the nuts were off it just slid out. But it took another hour or so to manoeuvre the engine out of the frame.

Having parted the engine and gearbox I could see the problem, the stud wasn’t tightened in the body enough when I attacked it with the wrench, consequently the threads were just ripped out. I now had several thoughts on who to blame, the first to get it was 'next doors cat', it looked at me and I looked at it, cats must be able to read human thoughts as it ran off very quickly when I scowled at it. The next thoughts were how to repair it, one - liquid metal or two - Helecoil it. To make a proper job of it I went to see Zak in Salisbury who just happened to have the right kit for the job. I think Zak has the right kit for just about everything, if he hasn’t got it he’ll make it!

Never having used a helicoil I was quite impressed how they work. Once you screw them into a hole they won't unscrew, a good piece of kit that I shall acquire.

Now, before the engine is returned to the frame I check all studs and nuts for their strength  (you tend to learn very quickly from your mistakes), all was well and a new confidence returned. I won’t bore you with the traumatic events getting the engine back into the frame without chipping the paintwork as I’m sure you’ve been there - only to say the truss needs replacing for a tighter one, given rest the voice will come back down to its normal level and the red colour in my face should change once the pills take affect.

I quickly re-fitted the diff and placed the back wheel into place. I thought that was it, all was in place and my confidence was fully charged again. After working on the various parts of the bike I noticed that the rubber drive coupling was quite close to the frame, in fact it was very close. I sat there and pondered what may be the trouble and it dawned on me that the drive shaft was not in properly. The spring clip on the end of the splined end was on the bottom adjustment and allowed the ends in the coupling to slide backwards. OUT came the diff again! And I pushed the spring to the top of the three adjustments, and to my surprise when the dif was in place it was right. There now is a good ¼ inch between the coupling and the frame, problem solved.

I had to go into inventive mode for the brake light switch as I could no longer get the original one. I have been told that they are as rare as “chickens teeth” or “rocking horse s - - -“, anyway I can’t find one, well not the same size anyway. Having a few small sheets of stainless steel plate around, and it is proper stainless. Some so called stainless metals tend to rust after a few months, but I have got some of the good stuff – (sounds like moonshine liquor,   “The Good Stuff”), sorry I digress. I happen to have a few brake light switches around and the one you see is off a Royal Enfield, it is slightly better quality than the Ural switch, but I have a Ural switch just in case this ones dies.

Using the rear footrest shaft I bent a piece of the stainless into a few right angles to get the right distance and to align with the rear brake linkage. I then drilled and tapped the pivot on the brake linkage and inserted a screw that fitted over another fashioned piece of stainless. As you can see the spring that came with the switch fits neatly onto the pivot. Now when the brake is pushed the brake switch is activated. I awarded myself a silver star for that. To keep in Russian mode, fine adjustments on the switch require the use of a large pair of pliers and bend the spring to suit.

 

 

 

 

 

 

 

 

 

 

 

 

 

 

 

 

 

 

 

 

 

 

 

 

 

 

 

Page 14
Page 15
Page 16
Chapter 4

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Last modified: 03/04/2008